525
Troubleshooting Tables
Section 12-1
19
Origin search
cannot be
executed.
An error or warning has been
generated.
Check the contents of the error
or warning.
If there is an error or
warning, then follow the
instructions.
20
The MC Unit’s origin proximity
input is wired incorrectly.
Use the Teaching Box’s input
signal monitor function to check
whether the sensors are turning
ON and OFF normally.
Correct the wiring.
21
The Servo Driver phase Z is
incorrectly wired to the MC
Unit.
Check the phase Z wiring.
Correct the wiring.
22
The direction of rotation does
not match the direction of the
limit input.
If axis rotation is reaching the
mechanical limit without revers-
ing direction, use the Teaching
Box to check whether the limit
inputs are turning ON and OFF
normally.
Correct the limit input
wiring.
23
The limit input is wired
incorrectly.
Check the limit input wiring.
Correct the limit input
wiring.
24
Origin search cannot be
executed because the Unit is
in Automatic Mode.
Monitor the Automatic Mode Bit.
Set the mode to Program Mode
and forcibly set only the Servo-
lock Bit.
Set the mode to
Automatic Mode and then
execute servo-lock.
(Change the ladder
program.)
25
Instructions cannot be
received from the ladder
program because the
Teaching Box is in T. BOX
ENABLED or T. BOX
RESERVED Mode.
Disconnect the Teaching Box
and check again.
Disconnect the Teaching
Box or put the Teaching
Box into T. BOX LIMITED
Mode.
26
Another axis control bit is ON
at the same time.
Check whether another axis
control bit is ON at the same
time.
Try executing origin using the
Teaching Box.
Turn OFF the other axis
control bit and turn ON
the origin search bit.
(Change the ladder
program.)
27
Not entering the in-position
range.
Is the MC parameter’s
in-position width too narrow?
Is the Servo Driver gain too low?
Is the servo speed reference
offset incorrect?
Increase the MC
parameter’s in-position
width.
Increase the Servo
Driver/MC Unit gain.
Adjust the servo speed
reference offset (zero
balance).
28
The low-speed origin search
feed rate is too fast.
Check the low-speed origin
search feed rate.
Decrease the low-speed
origin search feed rate.
29
The parameters are set
incorrectly.
Check the MC Unit parameters
with the CX-Motion.
If the single-direction mode is
specified for a system in which
limits are set for both sides, for
example, an error will occur and
operation will stop when a limit is
detected.
Set the parameters
correctly, transfer them to
the MC Unit, and write
them to flash memory.
30
The MC Unit is defective.
---
Replace the MC Unit.
No.
Problem
Probable causes
Items to check
Remedy
Summary of Contents for CS1W-MC221 -
Page 1: ...Motion Control Units Cat No W359 E1 04 CS1W MC221 V1 421 V1 OPERATION MANUAL ...
Page 2: ...CS1W MC221 V1 421 V1 Motion Control Units Operation Manual Revised February 2008 ...
Page 3: ...iv ...
Page 5: ...vi ...
Page 11: ...xii ...
Page 15: ...xvi ...
Page 19: ...xx ...
Page 27: ...xxviii Conformance to EC Directives 6 ...
Page 133: ...106 Installation Section 2 2 2 2 4 Dimensions CS1W MC421 CS1W MC221 ...
Page 173: ...146 Connecting Peripheral Devices Section 2 7 ...
Page 227: ...200 Command Area Section 3 6 ...
Page 351: ...324 Interface Specifics Section 5 4 ...
Page 513: ...486 Absolute Encoder Interface Specifications Section 9 7 ...
Page 575: ...548 Error Log Section 12 6 ...
Page 589: ...562 Performance Appendix A ...
Page 655: ...628 Control Bit Flag Timing Charts Appendix E ...
Page 683: ...656 Origin Search Patterns Appendix F ...
Page 685: ...658 Encoder Divider Rate and Rotation Speed for OMRON Servo Drivers Appendix G ...