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8-431
2
CPU1 detected an inconsistency
of emergency stop signal in robot
controller.
Connection failure
(1)Reset the alarm.
(2)If the alarm occurs again, check the followings.
·Confirmation of wiring for pin numbers A1, A2, B1, and B2 of YSU unit
(CN208 connector) and emergency stop SW of robot controller
Hardware failure
(1)Reset the alarm.
(2)If the alarm occurs again after confirming the connection, execute the
following contents. Save the CMOS.BIN before replacing the YSU unit to be
safe.
·Replacement of the emergency stop button on the robot controller
·Replacement of YSU unit
·Replacement of the emergency stop button on the robot controller and the
cable that connects to the YSU unit
3
CPU1 detected an inconsistency
of external emergency stop signal.
Connection failure
(1)Reset the alarm.
(2)If the alarm occurs again, check the followings.
·Wiring confirmation of YSU unit (CN216 connector) and pin numbers 19, 20,
21, and 22 of MXT terminal block
4
CPU1 detected an inconsistency
of external enable switch signal.
Connection failure
(1)Reset the alarm.
(2)If the alarm occurs again, check the followings.
·Wiring confirmation of YSU unit (CN216 connector) and pin numbers 33, 34,
35, and 36 of MXT terminal block
5
CPU1 detected an inconsistency
of safeguarding signal.
Connection failure
(1)Reset the alarm.
(2)If the alarm occurs again, check the followings.
·Wiring confirmation of YSU unit (CN216 connector) and pin numbers 9, 10,
11, and 12 of MXT terminal block
Alarm
Number
Alarm Name
Sub
Code
Meaning
Cause
Remedy
Содержание MOTOMAN DX100
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