Publication 2094-UM001A-EN-P — September 2006
Troubleshooting the Kinetix 6000 Drive System
149
E37
PowerPhaseLoss
Fault
(Phase Loss Flt)
•
One or more phases of the input ac power is missing.
•
Axis was enabled when main (three-phase) power was removed.
•
Common bus follower axis was enabled when dc bus power was
removed.
•
Check input ac voltage on all phases.
•
Disable axis before removing power.
E38
SERCOSFault
(SERCOS Ring Flt)
The SERCOS ring is not
active after being active
and operational.
Cable disconnected.
Check that fiber-optic cable is present and
connected properly.
E39
DriveHardFault
(Self Sense Flt)
Self-sensing Commutation
Startup Error
Motion required for self-sensing startup
commutation was obstructed.
•
Verify that there are no impediments to
motion at startup, such as hard limits.
•
Increase self-sensing current if high
friction or load conditions exist.
•
Check motor or encoder wiring using
wiring diagnostics.
E43
DriveEnableInput
Fault
(Drive Enable Flt)
Missing Drive Enable Input
Signal
•
An attempt was made to enable the
axis through software while the Drive
Enable hardware input was inactive.
•
The Drive Enable input transitioned
from active to inactive while the axis
was enabled.
•
Disable the Drive Enable Input fault.
•
Verify that Drive Enable hardware input
is active whenever the drive is enabled
through software.
E49
DriveHardFault
(Safe-off HW Flt)
Safe-off function
mismatch. Drive will not
allow motion.
•
Loose wiring at SO connector.
•
Cable/header not seated properly in
SO connector.
•
Safe-off circuit m24V dc.
•
Verify wire terminations, cable/header
connections, and +24V.
•
Reset error and run proof test.
•
If error persists, return the drive to
Rockwell Automation.
E50
SERCOSFault
(SERCOS Same ADDR)
Duplicate node address detected on SERCOS ring.
Verify that each SERCOS drive is assigned
a unique node address.
E54
DriveHardFault
(Ifbk HW Fault)
Current feedback hardware fault detected.
Replace the module
E60
DriveHardFault
(Unknown Axis)
Illegal ID bits detected
Replace the module
E61
AuxFeedbackFault
(Aux Fdbk AQB)
Auxiliary Encoder State
Error
The auxiliary encoder encountered an
illegal transition.
•
Use shielded cables with twisted pair
wires.
•
Route the feedback away from
potential noise sources.
•
Check the system grounds.
•
Replace the motor/encoder.
E62
AuxFeedbackFault
(Aux Fdbk Loss)
The feedback wiring is open, shorted, or missing.
Check the motor feedback cable
connectors/wiring to the IAM/AM and
motor.
E63
AuxFeedbackNoise
(Aux Fdbk Noise)
Noise on auxiliary
feedback cable.
Recommended grounding, per
installation instructions, has not been
followed.
•
Verify grounding.
•
Route feedback cable away from noise
sources.
•
Refer to System Design for Control of
Electrical Noise Reference Manual,
publication GMC-RM001.
E64
MotorFeedbackNoise
(Mtr Fdbk Noise)
Noise on motor feedback
cable.
E65
No Fault Message
(condition indicated
by on-screen
message)
(Hookup Fault)
Hookup procedure failed
Motor or feedback device malfunction.
•
Check motor power/feedback wiring.
•
Refer to on-screen message for
resolution.
Error
Code
Fault Message
RSLogix
(HIM)
Problem or Symptom
Potential Cause
Possible Resolution
Summary of Contents for Allen-Bradley Kinetix 6000
Page 8: ...Publication 2094 UM001A EN P September 2006 8 Table of Contents...
Page 18: ...Publication 2094 UM001A EN P September 2006 18 Start...
Page 118: ...Publication 2094 UM001A EN P September 2006 118 Connecting the Kinetix 6000 Drive System...
Page 190: ...Publication 2094 UM001A EN P September 2006 190 Specifications and Dimensions...
Page 265: ...Publication 2094 UM001A EN P September 2006 265 Notes...
Page 266: ...Publication 2094 UM001A EN P September 2006 266 Notes...
Page 267: ...Publication 2094 UM001A EN P September 2006 267 Notes...