BUS Updated 12/2011
07/2011
2-767
WorkCentre 5335 Family Service Documentation
047-211, 047-213
Status Indicator RAPs
Initial Issue
047-211 Exit 1 OCT Home Fail RAP
BSD-ON:
BSD 10.6 - Exit 1 Drive/OCT Control
After the Exit 1 OCT Motor has run for the specified operation time, the Exit 1 OCT Home Posi-
tion Sensor does not turn ON.
NOTE: When turning the power OFF, turn OFF the power switch first and then the main power
switch.
Initial Actions
•
Check the Exit 1 OCT Home Position Sensor for improper installation, contamination, and
etc.
•
Check the Shielding Board, which blocks the detection section of the Exit 1 OCT Home
Position Sensor, for damage and check the OCT Chute for improper installation.
Procedure
Turn the power ON and enter the Diag mode.
Turn ON
Component Control
[077-102] (Exit 1 OCT Home Position Sensor). Move the OCT
Chute manually to block/clear the light path to the Exit 1 OCT Home Position Sensor. Does
the display change between High/Low?
Y
N
Go to
BSD 10.6 - Exit 1 Drive/OCT Control
to check the Exit 1 OCT Home Position Sen-
sor (
PL 17.1
) for an open or short circuit.
Press the Stop button. Turn ON
Component Control
[077-010] and
Component Control
[077-
011] alternately. Does the OCT 1 Chute move forward and backward?
Y
N
Remove the Rear Lower Cover. Is the voltage between the MCU PWB
P/J417
-11/12
(+) and the GND (-) +24VDC?
Y
N
Go to
+24VDC Power RAP
.
Turn the power OFF and check the Exit 1 OCT Motor Gear for blockage and the OCT
Chute for damage. Also, check the connection between the MCU PWB
P/J417
and the
Exit 1 OCT Motor
P/J217
for open circuit, short circuit, and poor contact.
If no problems are found, replace the following parts in sequence:
•
Exit 1 OCT Motor (
PL 17.1
)
•
MCU PWB (
PL 18.2
)
Press the Stop button. Turn the power OFF and replace the MCU PWB (
PL 18.2
).
047-213 Finisher Type Mismatch
BSD-ON:
BSD 3.6 - IOT-Finisher Communication
Finisher type connected is incorrect.
Procedure
Ensure that the finisher connected is the proper Finisher.