Error no.
Error text
Error cause
M S
590
RV1/RV2:Change
Fault:
Change the direction speci
fi
cation during active travel
Additional information:
Display of the set direction
1 = RV1
3 = RV2
Remedy:
Check control of travel directions
●
●
13.5.9
Error 7xx
•
Trip abort due to errors between frequency inverter and control system
Error no.
Error text
Error cause
M S
710
DCP: Timeout
Error: DCP communication interrupted during travel
Remedy:
check wiring (shields)
●
●
715
DCP: G0-G7 fail !
Error:
Transmission error in the DCP protocol: Telegram for the speed preset
(G0-G7) not received
Remedy:
Possibly the DCP-function of the elevator control is not compatible
●
●
720
DCP: Delay fail
Error:
The DCP residual path increases during deceleration by more than 5cm
Remedy:
Check the absolute rotary encoder for its residual path determination
Wrong residual path signal from open loop control
●
●
721
DCP: Dist. fail
Fault:
There is no change in the residual path for 200 ms during the run
Remedy:
Check the absolute rotary encoder for its residual path determination
Wrong residual path signal from open loop control
●
●
722
DCP: s_rest = 0?
Error:
Residual path > 20mm jumps to 0mm
Remedy:
Check the absolute rotary encoder for its residual path determination
Wrong residual path signal from open loop control
●
●
723
DCP: s_rest < 0!
Error:
A negative residual path is transmitted during travel
Remedy: Check the DCP wiring
●
●
780
DCP: Quick Start >20s
Error:
In the quick start function, input "V=0" is triggered for over 20s
Remedy:
Shorten the time in which "V=0" is triggered
●
●
781
v0 at travel ?!l
Error:
Input "V=0" is triggered during travel
Remedy:
Check the triggering of "V=0"
●
●
799
RF:Failure
Error:
Control enable RF was switched off during travel (error evaluation only if
error no. 799 is entered in the error mask)
Remedy:
Check the triggering of "RF"
●
●
13.5.10
Error 8xx
•
Errors which can occur in operation with CANopen Lift
If an error occurs during operation with CANopen, the frequency inverter runs through status "ST_De-
lay" and
fi
nally goes to status "Wait drivecom. off". At this status the frequency inverter waits until the
control system sends the command "Fault Reset".
Error no.
Error text
Error cause
M S
800
CAN: Timeout
Errors in Velocity Mode:
Heartbeat from control system is missing or at wrong time.
Errors in Position Mode:
Heartbeat from control system and/or encoder is missing or at wrong time.
Adjustment:
Check CAN-connection
Check if devices have the right heartbeat.
●
810
CAN: Quick Stop Det.
Error:
Control system activates a quick stop.
820
CAN: Illegal Status
Error:
Control system sends commands in wrong order.
Adjustment:
Take care to the right order in CAN drive cycle
●
Original operating instructions
ZETADYN 3C
Error diagnosis
R-TBA08_03-GB 1619
Part.-No. 00163322-GB
145/204
Содержание ZETADYN 3C
Страница 196: ...Original operating instructions ZETADYN 3C EU declaration of conformity R TBA08_03 GB 1619 Part No 00163322 GB 196 204...
Страница 197: ...Original operating instructions ZETADYN 3C EU declaration of conformity R TBA08_03 GB 1619 Part No 00163322 GB 197 204...
Страница 198: ...Original operating instructions ZETADYN 3C EU declaration of conformity R TBA08_03 GB 1619 Part No 00163322 GB 198 204...
Страница 199: ...Original operating instructions ZETADYN 3C EU declaration of conformity R TBA08_03 GB 1619 Part No 00163322 GB 199 204...
Страница 200: ...Original operating instructions ZETADYN 3C EU declaration of conformity R TBA08_03 GB 1619 Part No 00163322 GB 200 204...
Страница 203: ...Original operating instructions ZETADYN 3C R TBA08_03 GB 1619 Part No 00163322 GB 203 204...