10.1 Troubleshooting
10-15
A.bF0
System Alarm
0
Occurred when the
control power
supply was turned
ON.
A SERVOPACK board fault occurred.
Replace the SERVOPACK.
A.bF1
System Alarm
1
A.bF2
System Alarm
2
A SERVOPACK board fault occurred.
A.bF3
System Alarm
3
A.bF4
System Alarm
4
A.C10
Servo Overrun
Detected
Occurred when the
control power
supply was turned
ON.
A SERVOPACK board fault occurred.
Replace the SERVOPACK.
Occurred when the
servo was ON or a
reference was input.
The order of phase-U, -V, and -W in the servomotor
wiring is incorrect.
Correct the servomotor wiring.
An encoder fault occurred.
Replace the servomotor.
A SERVOPACK fault occurred.
Replace the SERVOPACK.
A.C80
Absolute
Encoder Clear
Error and Multi-
turn Limit
Setting Error
Occurred when the
control power
supply was turned
ON.
An encoder fault occurred.
Replace the servomotor.
A SERVOPACK board fault occurred.
Replace the SERVOPACK.
Occurred when an
encoder alarm was
cleared and reset.
An encoder fault occurred.
Replace the servomotor.
A SERVOPACK board fault occurred.
Replace the SERVOPACK.
A.C90
Encoder
Communicatio
ns Error
Occurred when the
control power
supply was turned
ON or during
operation.
The encoder wiring and the contact are incorrect.
Correct the encoder wiring.
Noise interference occurred due to incorrect encoder
cable specifications.
Use tinned annealed copper twisted-pair or
twisted-pair shielded wire with a core of at least
0.12 mm
2
(0.0002 in
2
).
Noise interference occurred because the wiring
distance for the encoder cable is too long.
The wiring distance must be 20m (65.6 ft) max.
A.C91
Encoder
Communicatio
ns Position
Data Error
The noise interference occurred on the signal line
because the encoder cable is bent and the sheath is
damaged.
Correct the encoder cable layout.
The encoder cable is bundled with a high-current
line or near a high-current line.
Correct the encoder cable layout so that no surge
is applied.
The FG varies because of the influence from
machines on the servomotor side, such as welder.
Make the grounding for the machine separately
from PG side FG.
A.C92
Encoder
Communicatio
ns Timer Error
Noise interference occurred on the signal line from
the encoder.
Take a measure against noise for the encoder
wiring.
Excessive vibration and shocks were applied to the
encoder.
Reduce the machine vibration or mount the
servomotor securely.
An encoder fault occurred.
Replace the servomotor.
A SERVOPACK board fault occurred.
Replace the SERVOPACK.
A.CA0
Encoder
Parameter
Error
Occurred when the
control power
supply was turned
ON.
An encoder fault occurred.
Replace the servomotor.
A SERVOPACK board fault occurred.
Replace the SERVOPACK.
Table 10.3 Alarm Display and Troubleshooting (Cont’d)
Alarm
Display
Alarm Name
Situation at Alarm
Occurrence
Cause
Corrective Actions
Содержание SGDS Sigma III Series
Страница 3: ...SGDS Sigma III Servo Amplifier User Manual for Mechatrolink II Communications...
Страница 21: ......
Страница 29: ...1 Outline 1 8 2 Connecting to SGMSH SGMGH Servomotors Power Supply Three phase 200VAC SGMGH Servomotor...
Страница 59: ...2 System Selection 2 5 4 Regenerative Resistors 2 28...
Страница 68: ...3 3 SERVOPACK Internal Block Diagrams 3 9 3 3 3 Three phase 200 V 1 0 kW...
Страница 82: ...3 7 Dimensional Drawings of Base mounted SERVOPACK Model SGDS 12A 12A 3 23 Three phase 1 5kW...
Страница 133: ...5 Wiring 5 7 2 Connecting Externally Regenerative Resistors 5 28...
Страница 229: ...7 Operation 7 7 4 Absolute Encoder Home Position Offset 7 38...
Страница 375: ...Sigma II User s Manual Index Index 8...