I2tActv
I2t protection
is active
I2t protection is active,
which limits your
maximum torque to the
nominal rated values of
the motor. See 0x200A:
I2t for configuration
parameters.
0x2350,
0x2351
Please check 0x200A: I2t and see
whether it's configured as
expected.
Regarding the I2t being triggered,
that indicates that the drive is
protecting the motor from
potential overheating. Please read
our documentation of I2t for more
information.
Homing errors
HmInvMth
Invalid homing
method
The value of 0x6098:
Homing method is
invalid or not supported.
0x6320 Please firstly check object 0x6098:
Homing method and see whether
the object is written as expected.
Please refer to our
homing methods are supported.
HmIvSwSt
Invalid Switch
State during
homing
The state of the homing
switch at the end of the
homing routine was
unexpected. This can
happen if the homing
switch deactivates before
the axis moves back into
the valid range of
motion.
0x5300 Ensure that the homing switches
remain active after the mechanics
hit them. Increasing the homing
acceleration (0x609A) may help
prevent overshoot after the switch
is activated.
Internal Errors
Intern01
Internal fault 1
Internal Error Code.
Please contact support.
0x5300 Please note down the information
regarding the occurence of the
error and reach Synapticon
technical support for further
investigation.
Intern02
Internal fault 2
Internal Error Code.
Please contact support.
0x5300
Intern03
Internal fault 3
Internal Error Code.
Please contact support.
0x5300
Filter cutoff frequency bounds
VeFiFcLo
Velocity filter
cut-off
frequency too
low
0x2021:2 Velocity
feedback filter Cutoff
frequency is lower than
the minimum limit.
0x6320 Please check 0x2021:2 Velocity
feedback filter: Cutoff frequency,
and make sure that the cutoff
frequency is configured higher
than the limit 5 Hz. Please check
the documentation of the object
for latest information.
Synapticon Documentation
© 2021 Synapticon GmbH | Daimlerstraße 26 | D-71101 Schönaich Documentation v 4.19.0 | Built 2022-02-01
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