
Troubleshooting, Diagnoses and Maintenance
153
Table 31
Trip condition, their possible causes and remedial action
Trip condition
Possible Cause
Remedy
Motor I
2
t
“I
2
t”
I
2
t value is exceeded.
-
Overload on the motor according to the
programmed I
2
t settings.
-
Check on mechanical overload on the
motor
or the machinery (bearings,
gearboxes,
chains, belts, etc.)
-
Change the Motor I
2
t Current setting
PTC
Motor thermistor (PTC) exceeds maximum
level.
NOTE: Only valid if option board PTC/PT100
is used.
-
Check on mechanical overload on the
motor or the machinery (bearings,
gearboxes, chains, belts, etc.)
-
Check the motor cooling system.
-
Self-cooled motor at low speed, too high
load.
-
Set PTC, menu [234] to OFF
Motor PTC
Motor thermistor (PTC) exceeds maximum
level.
NOTE: Only valid if [237] is enabled.
-
Check on mechanical overload on the
motor or the machinery (bearings,
gearboxes, chains, belts, etc.)
-
Check the motor cooling system.
-
Self-cooled motor at low speed, too high
load.
-
Set PTC, menu [237] to OFF
Motor lost
Phase loss or too great imbalance on the
motor phases
-
Check the motor voltage on all phases.
-
Check for loose or poor motor cable
connections
-
If all connections are OK, contact your
supplier
-
Set motor lost alarm to OFF.
Locked rotor
Torque limit at motor standstill:
-
Mechanical blocking of the rotor.
-
Check for mechanical problems at the
motor or the machinery connected to the
motor
-
Set locked rotor alarm to OFF.
Ext trip
External input (DigIn 1-8) active:
- active low function on the input.
-
Check the equipment that initiates the
external input
-
Check the programming of the digital
inputs DigIn 1-8
Ext Mot Temp
External input (DigIn 1-8) active:
- active low function on the input.
-
Check the equipment that initiates the
external input
-
Check the programming of the digital
inputs DigIn 1-8
Mon MaxAlarm
Max alarm level (overload) has been
reached.
-
Check the load condition of the machine
-
Check the monitor setting in section 11.6, page 132.
Mon MinAlarm
Min alarm level (underload) has been
reached.
-
Check the load condition of the machine
-
Check the monitor setting in section 11.6, page 132.
Comm error
Error on serial communication (option)
-
Check cables and connection of the
serial communication.
-
Check all settings with regard to the
serial communication
-
Restart the equipment including the
VSD
PT100
Motor PT100 elements exceeds maximum
level.
NOTE: Only valid if option board PTC/PT100
is used.
-
Check on mechanical overload on the
motor
or the machinery (bearings,
gearboxes,
chains, belts, etc.)
-
Check the motor cooling system.
-
Self-cooled motor at low speed, too high
load.
-
Set PT100 to OFF
Содержание F33 Series
Страница 1: ...TECO F33 Variable Speed Drive Instruction manual English Software version 4 2X...
Страница 3: ......
Страница 33: ...30 Getting Started...
Страница 51: ...48 Main Features...
Страница 53: ...50 EMC and Machine Directive...
Страница 59: ...56 Operation via the Control Panel...
Страница 65: ...62 Serial communication...
Страница 159: ...156 Troubleshooting Diagnoses and Maintenance...
Страница 165: ...162 Options...
Страница 179: ...176 Technical Data...
Страница 187: ...184 Menu List...