
Note
Action
Screws: Hex socket head cap
screw M4x20 12.9 Lafre
2C2B/FC6.9 (4 pcs)
Refit the screws and washers without fully
tightened.
4
Washers: Washer 4.3x10x2 steel
(4 pcs)
Tightening torque: 2.6 Nm ±10%
xx2100001178
Hang a strap to the motor.
5
xx2100001126
Use a handheld dynamometer hooking to the strap
and pull the dynamometer to make the tension
falling in the allowed force range.
Note
During the measurement, make sure that all inter-
ferences that may affect the force are removed.
Pay attention to the force application direction.
6
Fasten the screws to the recommended tightening
torque.
7
Used belt: 139
Use a sonic tension meter to measure the timing
belt tension.
8
New belt:110
xx1800002887
If the timing belt tension does not meet the require-
ment, loosen the motor screws and readjust.
9
Continues on next page
812
Product manual - IRB 920
3HAC075721-001 Revision: C
© Copyright 2022 ABB. All rights reserved.
5 Repair
5.7.3 Replacing the axis-3 motor sub-assembly
Continued
Summary of Contents for IRB 920
Page 1: ...ROBOTICS Product manual IRB 920 ...
Page 8: ...This page is intentionally left blank ...
Page 14: ...This page is intentionally left blank ...
Page 50: ...This page is intentionally left blank ...
Page 110: ...This page is intentionally left blank ...
Page 984: ...This page is intentionally left blank ...
Page 1000: ...This page is intentionally left blank ...
Page 1002: ...This page is intentionally left blank ...
Page 1006: ......
Page 1007: ......