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270
Check first when you have a trouble
5.5.7
Acceleration/deceleration is not smooth
5.5.8
Speed varies during operation
When the slip compensation is selected, the output frequency varies between 0 and 2Hz as with load fluctuates. This is a
normal operation and not a fault.
Check
points
Possible Cause
Countermeasures
Refer
to
page
Parameter
Setting
Acceleration/deceleration time is too short.
Increase acceleration/deceleration time.
Torque boost
(Pr. 0, Pr. 46)
setting is improper under V/F
control, so the stall prevention function is activated.
Increase/decrease
Pr. 0 Torque boost
setting value by
0.5% increments to the setting.
The base frequency does not match the motor
characteristics.
For V/F control, set
Pr. 3 Base frequency and Pr. 47 Second
V/F (base frequency)
.
For General-purpose magnetic flux vector control, set
Pr.
84 Rated motor frequency
.
Stall prevention function is activated due to a heavy
load.
Reduce the load weight.
—
Set
Pr. 22 Stall prevention operation level
higher according
to the load. (Setting
Pr. 22
too large may result in
frequent overcurrent trip (E.OC ).)
Check the capacities of the inverter and the motor.
—
Regeneration avoidance operation is performed
If the frequency becomes unstable during regeneration
avoidance operation, decrease the setting of
Pr. 886
Regeneration avoidance voltage gain
.
Check
points
Possible Cause
Countermeasures
Refer
to
page
Input
signal
Multi-speed command signal is chattering.
Take countermeasures to suppress chattering.
—
Load
Load varies during an operation.
Select General-purpose magnetic flux vector control.
Input
signal
Frequency setting signal is varying.
Check the frequency setting signal.
—
The frequency setting signal is affected by EMI.
Set filter to the analog input terminal using
Pr. 74 Input
filter time constant
.
Take countermeasures against EMI, such as using
shielded wires for input signal lines.
Malfunction is occurring due to the undesirable current
generated when the transistor output unit is connected.
Use terminal PC (terminal SD when source logic) as a
common terminal to prevent a malfunction caused by
undesirable current.
Parameter
Setting
Pr. 80 Motor capacity
setting is improper for the
capacities of the inverter and the motor for General-
purpose magnetic flux vector control.
Check the
Pr. 80 Motor capacity
setting.
Fluctuation of power supply voltage is too large.
Change the
Pr. 19 Base frequency voltage
setting (about
3%) under V/F control.
Hunting occurs by the generated vibration, for example,
when structural rigidity at load side is insufficient.
Disable automatic control functions, such as energy
saving operation, fast-response current limit function,
regeneration avoidance function, General-purpose
magnetic flux vector control, and stall prevention.
During the PID control, set smaller values to
Pr.129 PID
proportional band
and
Pr.130 PID integral time
.
During the PID control, set smaller values to
Pr.129
PID
proportional band
and
Pr.130 PID integral time
.
Lower the control gain, and adjust to increase the
stability.
—
Change
Pr. 72 PWM frequency selection
setting.
Others
Wiring length exceeds 30m when General-purpose
magnetic flux vector control is performed.
Perform offline auto tuning.
Wiring length is too long for V/F control, and a voltage
drop occurs.
Adjust
Pr. 0 Torque boost
by increasing with 0.5%
increments for low-speed operation.
Change to General-purpose magnetic flux vector
control.
Содержание FR-D710W-0.1K
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Страница 297: ...295 APPENDIX This chapter provides the APPENDIX of this product Always read the instructions before using the equipment ...
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