
© 2018 Avco Corporation. All Rights Reserved
Appendix D
November 2018
Page 497
TEO-540-C1A Engine Maintenance Manual
Fault ID
352
Fault Group
45
Fault Name
[FAULT: local ignition switch noise]
Fault
Description
Local Ignition Switch Noise Fault
Fault Lamp
FFL
Root Cause
This fault indicates the local ignition switch is noisy. The fault will become inactive if the
noise is reduced.
Troubleshooting Steps
1.
Inspect wires connected to switch for breaks or damage. Are wires broken or damaged? If yes, repair in
accordance with the aircraft maintenance manual. If no, go to step 2.
2.
Complete a continuity and short circuit test of the switch. If the continuity or short circuit check fails,
replace the switch. If the continuity and short circuit test check is good, go to step 3.
3.
Complete a continuity test of the harness from the switch connections to the ECU connector using the
engine system schematic. If the continuity check fails, isolate to affected harness by disconnecting the
airframe interface connection AF-P1. If the continuity fails between switch and AF-J1, repair cable in
accordance with aircraft maintenance manual. If the continuity fails between AF-P1 and ECU, contact
Lycoming Engines. If the continuity checks good, replace the ECU.
Fault ID
353
Fault Group
45
Fault Name
[FAULT: ignition switch
discrepancy]
Fault
Description
Local Ignition Switch Discrepancy
Fault
Fault Lamp
FFL
Root Cause
This fault indicates the ignition switch differs between primary and secondary channels
possibly due to a hardware issue
Troubleshooting Steps
1.
Is the fault active, or are there any active or logged ignition switch slew rate or circuit faults?
If yes, go to step 2.
2.
Inspect wires connected to switch for breaks or damage. Are wires broken or damaged? If yes, repair in
accordance with the aircraft maintenance manual. If no, go to step 2.
3.
Complete a continuity and short circuit test of the switch. If the continuity or short circuit check fails,
replace the switch. If the continuity and short circuit test check is good, go to step 4.
4.
Complete a continuity test of the harness from the switch connections to the ECU connector using the
engine system schematic. If the continuity check fails, isolate to affected harness by disconnecting the
airframe interface connection AF-P1. If the continuity fails between switch and AF-J1, repair cable in
accordance with aircraft maintenance manual. If the continuity fails between AF-P1 and ECU, contact
Lycoming Engines. If the continuity checks good, replace the ECU.
Fault ID
354
Fault Group
45
Fault Name
-Reserved-
Fault
Description
Fault Lamp
FFL
Root Cause
Troubleshooting Steps