8 - 4
8. TROUBLESHOOTING
Display
Name
Definition
Cause
Action
1. Wrong setting of parameter No.
PA02
Set correctly.
2. Built-in regenerative brake resistor
or regenerative brake option is not
connected.
Connect correctly
3. High-duty operation or continuous
regenerative operation caused the
permissible regenerative power of
the regenerative brake option to be
exceeded.
Checking method
Call the status display and check
the regenerative load ratio.
1. Reduce the frequency of positioning.
2. Use the regenerative brake option of
larger capacity.
3. Reduce the load.
4. Power supply voltage is abnormal.
MR-J3- B:260VAC or more
MR-J3- B1:More than 135VAC
Review power supply
Permissible
regenerative power
of the built-in
regenerative brake
resistor or
regenerative brake
option is exceeded.
5. Built-in regenerative brake resistor
or regenerative brake option faulty.
Change servo amplifier or regenerative
brake option.
30
Regenerative
alarm
Regenerative
transistor fault
6. Regenerative transistor faulty.
Checking method
1) The regenerative brake option
has overheated abnormally.
2) The alarm occurs even after
removal of the built-in
regenerative brake resistor or
regenerative brake option.
Change the servo amplifier.
1. Small acceleration/deceleration time
constant caused overshoot to be
large.
Increase acceleration/deceleration time
constant.
2. Servo system is instable to cause
overshoot.
1. Re-set servo gain to proper value.
2. If servo gain cannot be set to proper
value:
1) Reduce load inertia moment ratio; or
2) Reexamine acceleration/
deceleration time constant.
31
Overspeed
Speed has
exceeded the
instantaneous
permissible speed.
3. Encoder faulty.
Change the servo motor.
1. Short occurred in servo motor power
(U, V, W).
Correct the wiring.
32
Overcurrent
Current that flew is
higher than the
permissible current
of the servo
amplifier.
2. Transistor (IPM) of the servo
amplifier faulty.
Checking method
Alarm (32) occurs if power is
switched on after U,V and W are
disconnected.
Change the servo amplifier.
3. Ground fault occurred in servo motor
power (U, V, W).
Correct the wiring.
4. External noise caused the
overcurrent detection circuit to
misoperate.
Take noise suppression measures.
Содержание MR-J3-B
Страница 1: ...General Purpose AC Servo MODEL MR J3 B SERVO AMPLIFIER INSTRUCTION MANUAL SSCNET Compatible J3 Series ...
Страница 13: ...A 12 MEMO ...
Страница 41: ...2 6 2 INSTALLATION MEMO ...
Страница 141: ...7 16 7 SPECIAL ADJUSTMENT FUNCTIONS MEMO ...
Страница 215: ...11 52 11 OPTIONS AND AUXILIARY EQUIPMENT MEMO ...