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5/2011
2-61
Phaser 4600/4620 Printer Service Manual
12-715-00, 12-716-00, 12-725-00, 12-726-00
Status Indicator RAPS
Revision - Xerox Internal Use Only
12-715-00, 12-716-00 Front Jogger Home Fault RAP
12-715-00 The left tamper did not move from home position as indicated by the Left Tamper
Home Position Sensor.
12-716-00 The left tamper did not move to home position as indicated by the Left Tamper
Home Position Sensor.
BSD-Reference:
WD 17
Initial Actions
•
Check for obstructions blocking tamper motion.
•
Cycle system power.
Procedure
WARNING
Switch off the electricity to the machine. Disconnect the power cord from the customer
supply while performing tasks that do not need electricity. Electricity can cause death or
injury. Moving parts can cause injury.
NOTE: Remove the Finisher top cover,
REP 12.18
to access the tamper motor and left cover
REP 12.1
to access the Left Tamper Home Position Sensor.
Select
dC330
code 12-815 to test the Left Tamper Home Position Sensor. The sensor signal
changes (high/low).
Y
N
Remove the Finisher,
GP 14
to check the condition of the Finisher option connector, sen-
sor and harness. The sensor is connected and the harness undamaged.
Y
N
Replace the sensor (
REP 12.10
), or repair the harness.
Replace the Finisher Control Board,
REP 12.2
.
Select
dC330
code 12-300 to test the tamper motor,
PL 12.35 Item 19
. The motor rotates
(on/off).
Y
N
Check the tamper motor connection and harness. Repair or reconnect as necessary.
Check the Finisher option harness in the Finisher Right Cover. The harness is undamaged.
Y
N
Repair the harness.
Replace these components in order until the error is corrected.
1.
IOT Upper Option Harness,
PL 10.30 Item 24
2.
MCU Board,
PL 3.10 Item 3
12-725-00, 12-726-00 Rear Jogger Home Fault RAP
12-725-00 The right tamper did not move from home position as indicated by the Right Tamper
Home Position Sensor.
12-726-00 The right tamper did not move to home position as indicated by the Right Tamper
Home Position Sensor.
BSD-Reference:
WD 17
Initial Actions
•
Check the stacker full sensor actuator.
•
Check for obstructions blocking actuator motion.
Procedure
WARNING
Switch off the electricity to the machine. Disconnect the power cord from the customer
supply while performing tasks that do not need electricity. Electricity can cause death or
injury. Moving parts can cause injury.
NOTE: Remove the Finisher top cover,
REP 12.18
to access the tamper motor and left cover
REP 12.1
to access the Left Tamper Home Position Sensor.
Select
dC330
code 12-820 to test the Right Tamper Home Position Sensor. The sensor sig-
nal changes (high/low).
Y
N
Remove the Finisher,
GP 14
to check the condition of the Finisher option connector, sen-
sor and harness. The sensor is connected and the harness undamaged.
Y
N
Replace the sensor (
REP 12.10
), or repair the harness.
Replace the Finisher Control Board,
REP 12.2
.
Select
dC330
code 12-320 to test the tamper motor,
PL 12.35 Item 19
. The motor rotates
(on/off).
Y
N
Check the tamper motor connection and harness. Repair or reconnect as necessary.
Check the Finisher option harness in the Finisher Right Cover. The harness is undamaged.
Y
N
Repair the harness.
Replace these components in order until the error is corrected.
1.
IOT Upper Option Harness,
PL 10.30 Item 24
2.
MCU Board,
PL 3.10 Item 3