background image

10

m

eChanICal

 

ComPonent

 

error

:

The bowl is too tight or too loose in the bowl arms.

 

Solution:

 “Adjustment of bowl clamping and centering”, 

page 12

The tool hits the sides of the bowl.

 

Solution: 

“Adjustment of bowl clamping and centering”

, page 12

Abnormal noise from the lifting actuator:

 

Solution: 

Lubrication of actuator; see lubrication chart on

 page 14

 

e

rror

 

CodeS

 

Shown

 

In

 

dISPlay

:

The error codes shown on the display are from the motor or the frequency transformer:

Motor error codes:

Code

Error

Solution

EE1

The CE switch interrupted the safety circuit when the 
mixer started

Check that the CE switch is closed with the bowl in the 
top position

EE2

The safety guard is open

If the guard is opened while the tool is not rotating, the 
error code will be eliminated when the guard is closed. If 
the guard is opened while the tool is rotating, closing the 
guard and pushing 

 will eliminate the error code.

EE3

The bowl is not correctly positioned, so the inductive 
sensor has not been activated

Check that the bowl is positioned correctly – if the bowl 
ring has three “ears”, the middle ear must point in towards 
the body of the mixer, otherwise the bowl must be lowered 
again and turned to the correct position. (It is possible to 
lower the bowl even if the error code is displayed.)

If/when the bowl is positioned correctly, push it right back 
into the bowl arms, the inductive sensor will then be acti-
vated and you can lift the bowl. 

If contact between the sensor and bowl is interrupted 
again, the error code will appear in the display. 

It is still possible to lift the bowl during the first 5 seconds 

when the error code is shown, after this the lifting move-
ment will be deactivated. 

Push the bowl right back into the bowl arms again so that 
contact is re-established between the bowl and sensor. The 
error code will disappear and you can lift the bowl again.

EE4

The thermal sensor in the motor has overheated

Reduce the quantity of ingredients in the bowl.

EE5

The overcurrent switch to the lifting motor has tripped.

Once the cause of the problem is found and the prob-

lem has been fixed, reset the overcurrent switch by 

pressing the blue button on the switch, see ill. The 
overcurrent switch is in the electrical box

Reason:

 The bowl arms have reached the physical 

end stop but the lifting motor has not cut out.

Check that the reed contacts, located on the outer tube 
of the lifting motor spindle, have been activated (the 
yellow diode on the contact illuminates) when the bowl 
arms are at the top or bottom.

If the reed contacts do not activate, they must be replaced

Reason: 

The bowl has too great a quantity of ingredi-

ents.

Reduce the quantity of ingredients in the bowl

EE6

The panel is not connecting with the frequency trans-
former.

Check the connection.

EE7

There is a fault with the frequency transformer.

Check the error log to ascertain the error code; 

see 

page 11

Summary of Contents for ERGO100

Page 1: ...bjerg S park 6 DK 2605 Br ndby Phone 45 43 44 22 88 info wodschow dk www bearvarimixer com Denmark ERGO60 ERGO100 ERGO140 AR200 VL 4 032017 ORDER NO 00453 GB Translation of the original user manual OP...

Page 2: ...a qualified electrician Of functional and safety reasons the machine must be connected to earth Contents The mixer must be bolted securely to the floor Load per leg not to exceed Voltage at the insta...

Page 3: ...lift the bowl the rest of the way VL 4 control panel with Remix function See page 5 for an explana tion of the panel Emergency stop Magnetic sensor which is activated by the guard when the guard is cl...

Page 4: ...aution as they destroy the mixer s lubricants Never use high pressure cleaning for the mixer Parts made of aluminum should not be used to strongly acidic highly alkaline or highly salty food stuffs wh...

Page 5: ...ible to store the entire recipe under a program number There are 20 program numbers 1 2 3 4 11 12 13 14 21 22 23 24 31 32 33 34 41 42 43 44 A program cannot be deleted but can be replaced The programs...

Page 6: ...X Thereispowerconnectiontothemixerandthebowlisnotinitstop position The bowl can be raised by activating the fields and simultaneously diodes in the fields are flashing The mixer cannot be started unti...

Page 7: ...er can be stopped by activating the field By activating the field the bowl is automatically lowered when the mixer stops The field has been activated and the mixer is ready The time can be changed by...

Page 8: ...an operation time for the mixer can be chosen by adjusting the time on and If the field is activated for longer time the speed is in creased reduced quicker Minutes and seconds are shown in the text...

Page 9: ...ay be necessary to lower the bowl in order to empty it Release the emergency stop to connect the power to the mixer Lower the bowl and empty it Now the mixer can be used as normal again How to bring a...

Page 10: ...into the bowl arms the inductive sensor will then be acti vated and you can lift the bowl If contact between the sensor and bowl is interrupted again the error code will appear in the display It is s...

Page 11: ...nsformer Reduce the quan tity in the bowl Oht1 IGBT overheating detected by internal sensor 22 Overloading of the frequency transformer Reduce the quan tity in the bowl Oht2 Internal braking resistor...

Page 12: ...ter and then measure the distance between beater and bowl edge By removing the rear covering the bowl arm guide plate is now accessible E Loosen the screws D and move the bowl arm guide plate in the r...

Page 13: ...and the right bowl arm resp is shown First find the bowl centering e g by mounting bowl and beater in the mixer and turn the beater round with your hand and measure the distance from the beater to the...

Page 14: ...14 Electrical components...

Page 15: ...15 Safety circuit...

Page 16: ...02 04 12 09 2016 4 6 01 CE CE 1 1 BU YEGN PK GY BN BK Wire code IEC EN 60757 PURPLE YEGN YELLOWGREEN OGBN ORANGEBROWN YEGN GY BN BK YEGN GY BN BK GY BN BK GY BN BK WH WH Main Motor PTO in motor Freque...

Page 17: ...side Tegningsnr Sagsnr Projekttitel Kunde Sidetitel Filnavn Sideref M lestok ERGO 140 6 26 01 06 2016 Diagram PC SCHEMATIC Automation 31 140 10 02 04 12 09 2016 5 7 01 CE CE 1 1 RDBK BUBK WHRD GYBK B...

Page 18: ...ine tuning the reed contacts and CE microswitch on page 19 The lifting actuator has 3 proximity detectors reed con tacts that check the position of the bowl Replacing the Reed contacts Remove the inco...

Page 19: ...corresponds to the top position of the bowl and the distance Y corresponds to the bottom position of the bowl The distances are measured from the underside of the bayonet shaft to the surface of the b...

Page 20: ...ad may only be re paired by an authorised technician During repairs Lifting actuator AK00131 Item D Fig 6 Always use spindle grease Mobilith SHC 460 from Mobil The gear of the actuator is lubri cated...

Page 21: ...s power must be disconnected Remove the machine s back plate by taking out the screws that hold it in place Preparation 100L 140L Remove the machine s lid Preparation 60L Loosen the earth cable If the...

Page 22: ...pprox 50 mm upwards so that it is free of the machine s lower bed Mark pins Release cables to the Reed switches on the actuator 60L 100L 140L Mark the three pins going to the three Reed switches on th...

Page 23: ...lation to marking Secure the cables Fit the guide plate for bowl arms 60L Place the guide plate for bowl arms in the machine and ensure that the marker pen lines and score marks on the plate and cross...

Page 24: ...se R hrmaschine D clare que le batteur m langeur ci dessous Verklaart hiermede dat Menger Declaramos que el producto batidora er i overensstemmelse med relevante bestemmelser i Maskindirektivet Direkt...

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