
6
Operation
Error list
Compact Operating Instructions – MOVITRAC
®
LTP-B
42
Code (in-
verter dis-
play)
Code
(MotionStudio
in P0-13)
Error code
status
word
if Bit5 = 1
CANopen
emergency
code
Meaning
Measure
Enc-09
38
0x0E
0x1026
HIPERFACE
®
type
is not supported.
During the use of Smart Servo Package, a wrong motor/
inverter combination was used. Check to see, if:
• The speed class of the CMP.. motor is 4500 min
-1
.
• The nominal motor voltage equals the nominal inverter
voltage.
• A HIPERFACE
®
encoder is being used.
Enc-10
39
0x0E
0x1027
Trigger: KTY
KTY has been triggered or is not connected.
Er-LED
Display error
Contact SEW‑EURODRIVE Service.
Err-SC
The keypad lost
the communication
connection to the
inverter.
Etl-24
External 24 V sup-
ply
Line voltage supply not connected. The inverter is exter-
nally supplied with 24 V.
FAULtY
The communica-
tion between the
controller and the
power section is
interrupted
Contact SEW‑EURODRIVE Service.
F-Ptc
21
0x1F
0x1015
Motor protection
triggered
The connected motor protection sensor is defined in
P2-33
(PTC, TF, TH, KTY or PT1000), and connected to
analog input 2 (terminal 10).
FAN-F
22
0x32
0x1016
Internal fan error
Contact SEW‑EURODRIVE Service.
FLt-dc
13
0x07
0x320D
DC link ripple too
high.
Check the current supply.
Ho-trP
27
0x27
0x101B
Error during refer-
ence travel.
• Check reference cams.
• Check limit switch connection.
• Check reference travel type setting and the parameters
required for it.
Inhibit
STO safety circuit
open.
Check to see if the terminals 12 and 13 are connected
correctly.
Lag-Er
28
0x2A
0x101C
Lag error
Check the following:
• The encoder connection
• The wiring of encoder, motor, and line phases
• Whether the mechanical components can move freely
and are not blocked.
• Extend the ramps.
• Set a higher P component.
• Parameterize the speed controller again.
• Extend the lag error tolerance.
• Set PLC Prog Task Priority to 10 ms
• The inverter is operated in Derating and can no longer
provide the current for acceleration/constant travel.
I.t-trp
04
0x08
0x1004
Overload of in-
verter/motor
(l2t error)
Make sure that:
• The motor nameplate parameters are correctly entered
in
P1-07
,
P1-08
, and
P1-09
.
• In vector mode (
P4-01
= 0 or 1), the motor power factor
in
P4-05
is correct.
• Auto Tune has been performed correctly.
Check to see, if:
• The decimals flash (inverter overloaded), increase the
acceleration ramp (
P1-03
) or decrease the motor load.
• The length of the cable meets the requirements.
• The load can move freely and there are no blockages
or other mechanical faults (mechanically check the
load).
• The thermal motor protection to UL508C is activated in
P4-17.
• See also "Fault reset delay in the case of an O-I and
hO-I error".
ML
Phase failure
Input phase missing or voltage is outside the specified
range.
26879778/EN – 03/2021
Содержание MOVITRAC LTP-B
Страница 2: ...SEW EURODRIVE Driving the world...
Страница 47: ......