CNC8070
R
EF
. 0402
E
RROR
SOLUTIONS
Page 91 of 128
Errors 3000-3999
3709
'Error when refreshing Analog Inputs'
DETECTION
When reading analog inputs.
CAUSE
Failure in the cyclic reading process for analog intputs. This could probably be due
to problems in the COMPCI, CAN bus, analog input module, etc.
SOLUTION
Check the status of the CAN bus, analog input modules, connections, etc.
3710
'Position command values out of range'
DETECTION
During execution.
CAUSE
Overflow in the position command variable. The maximum value for SGN32 has been
exceeded.
SOLUTION
Check the parameter settings of the axes (Gain, ServoOff, Resolution, etc.
3711
'Error when refreshing CAN feedback readings'
DETECTION
From the position loop, when reading the feedback of the analog axes.
CAUSE
The feedback reading of the analog axes was not completed due to an error at the
CAN bus, failure at one of the feedback readings, feedback module or saturation at
the CAN bus.
SOLUTION
Solve the possible error at the CAN bus or feedback module or increase the
LOOPTIME if there is saturation at the bus.
3712
'Home search error with Gantry axes'
DETECTION
During execution. While searching home on Gantry axes.
CAUSE
It detected the home switch of the master axis before that of the slave.
SOLUTION
Adjust the position of the home switches of the Gantry axes. The first home switch
to be pressed must be the slave one.
3800
'Continuous jog feedrate equal to zero'
DETECTION
During execution or when changing to continuous jog mode.
CAUSE
The feedrate for continuous jog is zero. No manual feedrate V.G.FMAN has been
programmed and machine parameter JOGFEED is zero.
SOLUTION
Check axis machine parameter JOGFEED.
3801
'Distance or feedrate in incremental jog equal to zero'
DETECTION
During execution.
CAUSE
The feedrate or distance for incremental jog is zero. No manual feedrate V.G.FMAN
has been programmed and machine parameter INCJOGFEED is zero or machine
parameter INCJOGDIST is zero.
SOLUTION
Check axis machine parameters INCJOGFEED and INCJOGDIST.
3803
'The handwheel resolution cannot be zero'
DETECTION
While changing handwheel resolution.
CAUSE
The index selected from the jog panel or via PLC for parameter MPGRESOL[i] is zero.
SOLUTION
Check axis machine parameter MPGRESOL.
3804
'Handwheel index out of range (switch positions 1-3)'
DETECTION
While changing handwheel resolution.
CAUSE
An attempt has been made to set via PLC a handwheel position that is out of the
permitted range.
SOLUTION
Check the writing of PLC.MPGIDX from the PLC.
3805
'Zero feedrate or distance in incremental jog'
DETECTION
While changing the distances or feedrates of incremental jog.
CAUSE
The index of incremental jog has been changed using a PLC program or the jog panel.
The index selected for parameter INCJOGDIST or INCJOGFEED is zero.
SOLUTION
Check axis machine parameters INCJOGDIST and INCJOGFEED.
3806
'Incremental jog feedrate greater than the maximum value'
DETECTION
During execution.
CAUSE
The feedrate set by machine parameter for incremental jog is greater than the
maximum allowed.
SOLUTION
Check machine parameters MAXMANFEED, INCJOGFEED and G00FEED.
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