Section 5 - Procedures
TS200
5.3-6 Callibration Fault Codes
During calibration, the TS200 control module repeatedly checks for possible problems which might prevent
successful calibration, or subsequently give inaccurate platform load estimates.
If any problem is detected, a flashing error message is immediately displayed and calibration is terminated - the
problem must be resolved, and calibration re-started.
Fault Code List
Most calibration error messages have an "Fxx" number as well as a description, to aid in trouble-shooting:
Fault Code
I
Description
F01 :CANNOT RUN
Something is wrong, preventing the TS200 from running - check the HELP message (causes
include line contactor, valve, or motor wiring errors)
F02:NOT GROUND
Calibration can only be carried out from BASE control!
MODE
F03:NOT STOPPED
The machine must not already be moving when calibration is begun.
F04:TILTED
The machine must be on level ground when calibration is begun.
F05:BAD HEIGHT1
At the start of calibration, the EZfit height sensor is out of range (output must be between 0.9V and
F05:BAD HEIGHT2
4.1 V with platform fully lowered)
F06:CHECK ELEV
At the start of calibration, the ELEVATION switch (P4-6) is open with platform fully lowered
F07:BAD HEIGHTS
During calibration, the two height sensors disagreed too much
F0B:CHECK ELEV
The ELEVATION switch (P4-6) is closed with platform fully raised - or the switch changed state
more than once (it should go from closed to open just once, as the platform is raised)
F09:BAD HEIGHT1
The EZfit height sensor is out of range when fully lowered (0%) calibration is recorded (output must
F09:BAD HEIGHT2
be between 0.9V and 4.1 V with platform fully lowered)
F10:BAD HEIGHT1
The EZfit height sensor is out of range when fully raised (100%) calibration is recorded (output must
F10:BAD HEIGHT2
be between 0.6V and 4.4V with platform fully raised)
F11:NOT UP
When instructed to go up (raise the platform) the DOWN switch was activated, or vice-versa (check
F11 :NOT DOWN
switch wiring)
More than 500 samples were recorded during dynamic lifting - the machine lifts too slowly Increase
F12: TOO MANY
the value of SETUPS/HEIGHT SETUPS/SAMPLE@ to delay longer between each sample (do not
increase too much, as this will cause inaccurate dynamic load estimates
F13:LOW HEIGHT
There is not enough difference between the EZfit height sensor output when fully lowered, and fully
RANGE
raised (minimum allowed difference is 1 V)
Ensure the UP switch is not released before the platform is fully raised.
F14: BAD HEIGHT1
The EZfit height sensor output is bad during dynamic lifting (must be between 0.6V and 4.4V
always)
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Summary of Contents for 1330-ED
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Page 31: ...Section 3 System Component Identification and Schematics 31 1330ED 1530ED micro GMG...
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