Please note:gate moves only in “dead-man” mode if you have any of the messages
marked above (with this symbol:
*
) shown on the display
!
Please note:gate moves only in “dead-man” mode if you have any of the messages
marked above (with this symbol:
*
) shown on the display
!
12
Troubleshooting Guide
in
Parking and access control equipment manufactured in the UK
Automatic Sliding Gates
Message
Short description:
Cause of message
F.020
Run time exceeded (during opening,
closing or deadman)
• current motor run time has exceeded set maximum run time
(P.410 (Opening), P.415 (Closing), P.419 (Deadman move)), door
may be sticking or is blocked
• Door is blocked
• If using mechanical limit switches, one may not have tripped
F.030
Lag error (position change of the
door is less than expected)
• gate or motor is blocked
• insufficient power for providing necessary torque
• too little speed
• mechanical limit switch was not left or is defective
• Incremental or absolute encoder shaft is slipping
• wrong positioning system selected (P.205)
• one motor phase is missing
• the brake does not release
• Settings of the failure detecting time are not correct (P.430 or
P.450)
F.031
Detected rotational direction
deviates from expected
• When using incremental encoders: Channel A and B reversed
• Motor rotation direction reversed compared with calibration setting
? teach in the limits again (P.210 = 5)
• Too much „pancaking“ when starting, brake releases too soon, or
too little torque, adjust boost (P.140 or P.145) as necessary.
F.211
External E-Stop 1 tripped
• E-Stop chain was interrupted starting at Input 1
F.212
External E-Stop 2 tripped
• E-Stop chain was interrupted starting at Input 2
F.320
Obstacle during opening
• During opening an obstacle has recognized
F.325
Obstacle during closing
• During closing an obstacle has recognized
F.360
Short circuit detected on edge input
• Short circuit detected on edges with normally closed contact
F.400
Controller hardware reset detected
• Excessive noise on supply voltage
• Internal watchdog tripped
• RAM error
F.410
Over-current (motor current or DC-
bus)
• Wrong motor data set (P.100 – P.103)
• Non-adjusted voltage increase / boost set (P.140 or P.145)
• Motor not properly dimensioned for door
• Door sticks
F.425
Overvoltage line supply
• The supply voltage for the controller is to high
F.510
Motor / DC-bus overcurrent Limit 2
• Wrong motor data set (P.100 – P.103)
• Non-adjusted voltage increase / boost set (P.140 or P.145)
• Motor not properly dimensioned for door
• Door sticks
F.520
Overvoltage in DC-bus Limit 2
• Brake chopper interference / defective / missing
• Feed voltage much to high
• Motor feeds back too much energy in generator mode, door
motion energy cannot be sufficiently brought down.
F.521
Overvoltage in DC-bus
• Input voltage supply too low, usually at load
• Load too great / final stage or brake chopper fault
F.525
Overvoltage at the line supply input
• The line supply for the Controller is to high
• The line supply fluctuates very extremly
F.530
Heatsink temperature outside of working
range Limit 1
• Excessive load on final stages or brake chopper
• Ambient temperature too low for controller operation
• Clock frequency of final stage too high (Parameter P.160)
F.535
Housing temperature high
• The temperature inside the controller housing is to high
F.700
Impossible combination of Limits
• Both limit switches are active at the same time
F.930
External watchdog incorrect
• Defective hardware has been damaged by water or electric
Содержание FF9000
Страница 14: ...Wiring Diagram in Parking and access control equipment manufactured in the UK Automatic Sliding Gates 14 ...
Страница 17: ...Wireless Encoder in Parking and access control equipment manufactured in the UK Automatic Sliding Gates 17 ...
Страница 18: ...18 Wireless Encoder in Parking and access control equipment manufactured in the UK Automatic Sliding Gates ...