Smart Positioner
YT-1000 / 1050 series
Product Manual
Ver. 1.04
61
Linearity is too low.
1) Check if linear positioner is properly positioned. Especially check if the feedback lever is
parallel to the ground at 50% point.
2) Check if zero and span point have been properly adjusted. If either one of values is
being adjusted, another one must be re-adjusted as well.
3) Check if supply air pressure level is stable from the regulator. If the level is unstable, the
regulator must be replaced.
Hysteresis is too low.
1) In case of double acting actuator, check if seat adjustment has been properly performed.
Please contact YTC for any further inquiries regarding the seat adjustment.
2) Backlash can occur when the feedback lever and lever spring are loosen. To avoid
backlashing, please adjust the lever spring.
3) Check if the connection bar to the feedback lever is tightly fastened.
Содержание YT-1000 series
Страница 1: ...SMART POSITIONER PRODUCT MANUAL YT 1000 1050 SERIES VERSION 1 04 ...
Страница 19: ...Smart Positioner YT 1000 1050 series Product Manual Ver 1 04 19 2 7 3 YT 1000R 2 7 4 YT 1000R SPTM Internal ...
Страница 20: ...Smart Positioner YT 1000 1050 series Product Manual Ver 1 04 20 2 7 5 YT 1000R Limits Switch Internal ...
Страница 27: ...Smart Positioner YT 1000 1050 series Product Manual Ver 1 04 27 2 8 10 YT 1000R External SPTM with LCD ...
Страница 28: ...Smart Positioner YT 1000 1050 series Product Manual Ver 1 04 28 2 8 11 YT 1000R External Limit Switch ...