Code
Error message
Error reaction
Possible reason
E29
(0x31D)
Motor load too high (Motor I²t)
Motor is stopped by error ramp
and current limitation.
(1)
▶
Average motor load is too high due
to mechanical problems
▶
Wrong dimensioning of the motor
E30
(0x31E)
Power output stage load too high
(I²t)
Motor is stopped by error ramp
and current limitation.
(1)
▶
Average load of output stage is too
high due to mechanical problems
▶
Wrong dimensioning of the drive
E31
(0x31F)
Speed error or slip too great
SERVO / VECTOR: Drive is
limited by current monitoring via
short-circuit of the motor phases.
(1)
HSPWM: Drive is stopped by error
ramp and current limitation.
▶
Motor is not able to comply with the
set speed (e.g. defective motor,
mechanical problems, wrong para‐
meters), failure of the measuring
system
E33
(0x521)
Power supply load monitoring ->
mains voltage too high
Power supply unit will be discon‐
nected from mains.
▶
Parameterized mains voltage does
not match the connected voltage
▶
Device connected incorrectly
▶
Heavy fluctuation of the power
supply towards overvoltage
E34
(0x522)
Power supply load monitoring ->
mains voltage too low
Power supply unit will be discon‐
nected from mains.
▶
DC link was not precharged to the
minimum voltage level in the set
time period; mains voltage is
connected to the short-circuited DC
link
E35
(0x523)
Error in external power supply unit
Drive is immediately disabled,
motor coasts to standstill.
▶
Error message from external power
supply unit; power supply is
switched off.
E36
(0x524)
Encoder 0 monitoring
Motor is stopped by current moni‐
toring via short-circuit of the motor
phases.
▶
Connection of encoder 0 is faulty
▶
Broken cable
E37
(0x525)
Ballast circuit load (I²t ballast
resistor)
Drive is immediately disabled,
motor coasts to standstill.
Ballast circuit load due to:
1
I²t
1
Wrong dimensioning, too much
energy supplied to R
Ballast
, broken
cable, no bridge at R
Ballast
(int./
ext.)
2
(VCE) desaturation detection
or: DC DC converter over‐
load
(only 0362144xy)
2
Bridge at R
Ballast
is not correct,
short circuit of insulation etc.
Or: internal hardware fault
(only
0362144xy)
E37
(0x525)
DC DC converter overload
(only
0362161xy)
Power supply unit will be discon‐
nected from mains.
▶
Overload at voltage converter of
DC link
E38
(0x526)
Actual speed value greater than
overspeed threshold
Motor is stopped by current moni‐
toring via short-circuit of the motor
phases.
(1)
▶
Wrong parameters
▶
Motor connected incorrectly
E39
(0x527)
Tracking error monitoring and
motor slowdown
Motor is stopped by current moni‐
toring via short-circuit of the motor
phases.
(1)
▶
Wrong parameters
▶
Motor connected incorrectly
▶
Mechanical problems
E40
(0x528)
Motor feedback
Motor is stopped by current moni‐
toring via short-circuit of the motor
phases.
(1)
▶
Connection of motor feedback
faulty
▶
Broken cable
E41
(0x529)
Motor phase lost
Motor is stopped by current moni‐
toring via short-circuit of the motor
phases.
(1)
Motor connection/configuration is faulty:
1
No motor connected
1
No motor connected / incorrect
wiring, broken cable
2
Wrong motor connected
2
Wrong parameters
W
Error Messages
Drive System SD2 - Safety Functions SFM / SLOF
61
10
Содержание SD2
Страница 1: ...Drive System SD2 Safety Functions SFM SLOF P TD 0000426 12 2019 08 28 SIEB MEYER W ...
Страница 4: ...Chapter Overview W 4 Drive System SD2 Safety Functions SFM SLOF ...
Страница 10: ...General Information W 10 Drive System SD2 Safety Functions SFM SLOF 2 ...
Страница 16: ...Safe Frequency Monitor SFM W 16 Drive System SD2 Safety Functions SFM SLOF 3 ...
Страница 44: ...Fieldbus Communication W 44 Drive System SD2 Safety Functions SFM SLOF 6 ...
Страница 56: ...OSSD Signals W 56 Drive System SD2 Safety Functions SFM SLOF 8 ...
Страница 66: ...Error Messages W 66 Drive System SD2 Safety Functions SFM SLOF 10 ...