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ADSR modulation depth. Problems can first be traced to the LM324 U6, 
but proper functioning of this IC is assured if the output follows the input. 
The input levels on the resistor network associated with this summing 
amp should be checked for conformity with a good amp. Problems with 
the ADSR can be traced to the output buffers/demux circuit formed by 
U17 (TL064) and U4 (CD4051). The buffer outputs should have a DC 
level of about 7V, which is the ADSR sustain level. This will vary if the 
ADSR mod depth is changed on EDIT PAGE 2. Again, note that the F

c

 

modulation outputs should all be 0V. 

4.7.4  Step 11-27:  VCO Volume Test 

These steps check for proper operation of the SSM 2024 Quad VCA ICs 
U22 and U23. If problems occur, first try a new IC, then check the VCO 
volume control voltages generated by the buffers in U15 (TL064) which 
should be about 7-10V when the particular VCO is supposed to be on 
and 0V for VCO off. 

4.7.5  Step 28-31:  F

c

 & Q Modulation 

These steps check for proper operation of the F

c

 and Q modulation 

demultiplexer formed by CD4052 U1 and the associated TL068 buffers. 
The outputs of all the TL068s should have a sweeping LFO sawtooth if 
they’re functioning properly. If not, check if the CD4052 inputs (pins 3 & 
13) have sawtooths. If they do, check the buffers and scan the clocks on 
pins 6, 9 & 10 on the CD4052. 

4.7.6  Step 32-35:  VCO1 & 2 Modulation 

This is the same as Step 28-31, except it refers to U2 and has an LFO 
square wave output instead of sawtooth. 

4.7.7  Step 36-39:  Noise Audio Path 

This checks if the noise (generated on the MIXER) makes it through all 
four VCFs. If not, check the resistor pack inputs for noise. If it’s not there, 
check for shorts or see if the MIXER actually has noise coming out of it. 

4.7.8  Step 40-43:  VCO Bypass VCF 

The functioning of the MC14551 quad switch U14 is tested here. If the 
board passed the VCO volume tests and fails this test, then U14 is 
probably defective. Check, however, that the control pin 9 is actually 
working (this comes from the DAC) or else the switching won’t occur. 
You can do this by switching between STEP 40 and 39 to see if the 
voltage pin 9 toggles between 0V and 8V. 

4.7.9  Step 43:  TL068 Drift Test 

The TL068s serve as buffers for the modulation demultiplexers U1 and 
U2. If they are excessively noisy or have a high drift (which can be 

Summary of Contents for Voyetra Eight

Page 1: ...By Reason 1 0 1984 Carmine J Bonanno Original Revision 1 0a 06 19 2002 Joan Touzet joant ieee org http www atypical net Mistake correction Revisions for clarity Started schematic entry Copywright sic...

Page 2: ...10 2 3 HEADPHONES 11 2 4 NOISE 11 2 5 CALIBRATIONS 11 3 VCO CARD 12 3 1 THEORY OF OPERATION 12 3 2 VCO OPERATION 12 3 3 AUTOTUNE FUNCTIONALITY 13 3 4 DC VOLTAGES 14 3 5 CARD PIN SIGNALS 14 3 5 1 Input...

Page 3: ...N SYSTEM SCAN CLOCKS 24 5 4 DEMULTIPLEXING REMULTIPLEXING 24 5 5 MONO CONTROLLER MULTIPLEXER 25 5 6 MISCELLANEOUS SWITCHING FUNCTIONS 25 6 KEYBOARD 26 6 1 THEORY OF OPERATION 26 6 2 CIRCUIT OPERATION...

Page 4: ...pecific features Alternately the Quality Control Calibration test tape may be loaded into the instrument and the documented test procedure may be used to test all system functions for proper operation...

Page 5: ...fer to the VCO section of this manual A strange clicking or thumping is heard whenever a key is pressed Is the click part of a patch Play the null patch and see if it goes away Try turning off the VCO...

Page 6: ...tial filter resonance for each VCF 1 4 4 DAC Card Contains the Voice on off functions and the A D and D A functions which allow the CPU to control the analog system components Calibrations include DAC...

Page 7: ...e jacks and an AGC circuit for the Tape input 1 4 12 Power Supply Contains regulators and fuses for 15V 5V 11V 22V as well as power down detection circuitry for the battery backed up RAM on the CPU 1...

Page 8: ...w paths Mod Bank VCAs VCO1 VCO2 Fc Q 2 2 2 2 VCO1 VCO1 2 2 2 2 VCO2 VCO2 Mono Contr MIX VCO VCF VCO VCO VCF VCO DAC DIGI ANA1 ANA2 CPU POT x Press Mono Controllers Figure 1 2 Modulation System Signal...

Page 9: ...8 8 8 VCA VCA VCA VCF Cards Phones Volume Phones Out 15 Noise Gen MM5837 VCA 2 Vol L R Right Mono Left Master Outputs Buffers VCA VCA Programmable CPU Vol L Parameter Trim Volume CPU Vol R Buffer Exte...

Page 10: ...f two such that VCA 0 1 come from one op amp output VCA 2 3 from another op amp output and so on When the keyboard WHOLE 8 Mode is selected the output of sub mixer 0 1 is hard panned to one side of th...

Page 11: ...control voltage to this VCA to set the headphone volume 2 4 Noise The noise source is generated by an MM5837 digital noise generator This output is sent to two VCAs which set the noise L R volume and...

Page 12: ...te a square wave that is one octave below the oscillator frequency The waveforms are summed by an LF347 wide bandwidth op amp Since this summer is inverted it is followed by an inverter to form positi...

Page 13: ...correction voltage it has to send to the VCO Control Input to have it generate a frequency of 440Hz when the middle A key is pressed on the keyboard This voltage is added to the keyboard voltage when...

Page 14: ...oltages The card uses 15V to drive the CEM 3340s and opamp ICs The CEM 3340s also require a stable 5V reference which is derived on board to minimize system interaction between cards The 10V reference...

Page 15: ...e CEM3340 3 6 3 Step 74 75 Linear FM Check Linear FM is when the output of the VCO2 mixer is routed to the linear control current input on VCO1 Problems can be caused by the CD4053 switch or if the ou...

Page 16: ...an be caused by a bad CD4051 bad buffers or bad CEM3340 First switch the CD4051 with one on a voice that has no problems If the problem now appears on the other voice the CD4051 is bad Then try switch...

Page 17: ...ents of the VCO volume VCAs and the noise voltage dropped across the 100K noise input resistors while the output current is converted to a voltage by the voltage to current converter opamp inverter TL...

Page 18: ...tave change in filter frequency The control voltage is scaled down to less than 100mV at the SSM2044 input pin 13 to obtain the full sweep range of 20 Hz 20 kHz Filter resonance is determined by the c...

Page 19: ...he LF347 buffer amplifiers that precede the CD4052 inputs prevent the scanning clocks from leaking into the VCF audio inputs 4 5 DC Voltages The card uses 15 Volts to drive the SSM ICs and associated...

Page 20: ...n outputs from the CD4052 U7 and the four Fc modulation outputs should all be at 0 V Thus Q calibration problems where Q will not turn off should take this into account In steps 00 and 01 the Fc outpu...

Page 21: ...and the associated TL068 buffers The outputs of all the TL068s should have a sweeping LFO sawtooth if they re functioning properly If not check if the CD4052 inputs pins 3 13 have sawtooths If they d...

Page 22: ...ause the VCOs to jitter and sound unstable In this step the outputs of the TL068s are examined at a high scope sensitivity to weed out potentially bad ones The inputs to the CD4052s are all 0V so the...

Page 23: ...s to address these demultiplexers so that the proper analog signal may be refreshed when necessary Since the system uses 15V to bias these CD4051s the control signals including address and enable vary...

Page 24: ...by an M is encountered in the VOYETRA logic description e g MA0 it stands for modulation system signal Thus MA0 MA1 and MA2 are the modulation system address lines which are periodic square waves The...

Page 25: ...witching Functions The two CD4174 addressable latches are used by the CPU to address the POT PANEL parameter trimmers See the POT PANEL theory for an explanation of how these trimmers are accessed The...

Page 26: ...criptions in this section it would be best to review the POT PANTEL theory of operation since much of the explanations pertaining to the operation of the keyboard data and clock power lines is based o...

Page 27: ...6 and latches all of the edge triggered CD4021s connected to the LATCH UB latch upper bus line when the gate transition from low to high occurs Since state Q1 on the CD4015 is still low the LOEWR BUS...

Page 28: ...digital level translator CD4051 U8 and enables the analog multiplexer CD4051 U9 The ASTR also sets the outputs of the CD4024 divider to a low state addressing the first input of U9 which is the Y lin...

Page 29: ...ressure sensors gain adjustment for left and right pressure sensors gain adjustment for left and right pressure sensors and balance Joystick calibrations include offset adjustment for X and Y axes and...

Page 30: ...flip flop 74LS279 LOW When done the CPU writes to location 4 and sets the flip flop HIGH This DEMUXEN line drives a 16 channel demultiplexer on DIGIMOD that drives all of the system CD4051s In normal...

Page 31: ...ators are driven by the unregulated 21V supply which is fused on the power supply board In normal operation the clock power line should always be active Since the CPU demands information from the keyb...

Page 32: ...rther processed by the analog circuitry that follows the LM324 U16 buffers The CD4053 switches allow the VOYETRA to be controlled by a slave when they are switched to the external positions This is se...

Page 33: ...ules Thus the trimmer diode network that follows the pitch bend buffer allows balance to be set while the gain controls for pitch bend left and right adjust for pitch bend range uniformity in both lef...

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