6.10 Fine Tuning during Test Runs (Adjust the Control Function)
504
YASKAWA
TOEPYAIGA8001B GA800 Drive Maintenance & Troubleshooting
Issue
Parameter Number
Possible Solutions
Default
Recommended Setting
Hunting or oscillation
C5-06 [ASR Delay Time]
•
If torque or speed response are
slow, decrease the setting value
in increments of 0.010.
•
If the rigidity of the machine is
unsatisfactory and vibration is
possible, increase the setting
value.
0.004 s
0.004 s to 0.020 s
When you operate the drive at a
frequency close to zero speed, the
motor rotates at a frequency
slightly higher than the frequency
reference.
•
E1-09 [Minimum Output
Frequency]
•
n4-70 [Speed Command Comp
@ Low Freq]
•
Set
E1-09 > 0
.
Note:
When frequency reference
E1-
09 < 0
, the drive output will
turn OFF.
•
Decrease the setting value of
n4-70
in 0.1 Hz increments.
Note:
If you set the value too low,
the motor can rotate in reverse.
•
E1-09 = 0.0 Hz
•
n4-70 = 1.00 Hz
•
E1-09 = 0.5 Hz
•
n4-70 = 0.50 Hz
*1
The default setting changes when the settings for
C6-01 [Normal / Heavy Duty Selection]
and
o2-04 [Drive Model (KVA) Selection]
change.
*2
The default setting changes when the setting for
o2-04 [Drive Model Selection]
changes.
*3
Refer to the section on
C5-xx parameters
for more information about speed control (ASR).
*4
The best values for a no-load operation are different than the best values for actual loading operation.
◆
Open Loop Vector Control for PM Motors
Table 6.21 Parameters for Fine Tuning the Drive (
A1-02 = 5 [OLV/PM]
)
Issue
Parameter Number
Possible Solutions
Default
Recommended Setting
Unsatisfactory motor performance
E1-xx parameters, E5-xx
parameters
•
Check the settings for
E1-06,
E1-04 [Base Frequency,
Maximum Output Frequency]
.
•
Check the
E5-xx
and make sure
that you set all motor data
correctly.
Note:
Do not set
E5-05 [PM Motor
Resistance (ohms/phase)]
to a
line-to-line resistance value.
•
Do Auto-Tuning.
-
-
Unsatisfactory motor torque and
speed response
n8-55 [Motor to Load Inertia
Ratio]
Adjust to align the load inertia
ratio of the motor and machine.
0
Near the load inertia ratio.
n8-45 [Speed Feedback Detection
Gain]
Decrease the setting value in
increments of 0.05.
0.80
-
C4-01 [Torque Compensation
Gain]
Adjust the setting value.
Note:
If you set this value too high, it
can cause overcompensation
and motor oscillation.
0.00
1.00
•
Oscillation when the motor
starts.
•
Motor stalls.
n8-51 [Pull-in Current @ Accel/
Decel]
Increase the setting value in
increments of 5%.
50%
-
•
b2-02 [DC Injection Braking
Current]
•
b2-03 [DC Inject Braking Time
at Start]
Use DC Injection Braking at start.
Note:
This can cause the motor to
rotate in reverse for
approximately 1/8 of a turn at
start.
•
b2-02: 50%
•
b2-03: 0.00 s
•
b2-02: Adjust as necessary.
•
b2-03: 0.5 s
n8-55 [Motor to Load Inertia
Ratio]
Increase the setting value.
Note:
When you operate a single
motor or with a minimum
quantity of inertia, if you set
this value too high, it can cause
motor oscillation.
0
Near the load inertia ratio.
There is too much current during
deceleration.
n8-79 [Pull-in Current at
Deceleration]
Set
n8-79
<
n8-51
.
50%
Note:
When
n8-79 = 0
, the drive will
apply the
n8-51
setting to the
pull-in current during
deceleration.
Decrease in increments of 5%.
Summary of Contents for GA800 Series
Page 2: ...This Page Intentionally Blank 2 YASKAWA TOEPYAIGA8001B GA800 Drive Maintenance Troubleshooting...
Page 18: ...i 2 Using the Product Safely 18 YASKAWA TOEPYAIGA8001B GA800 Drive Maintenance Troubleshooting...
Page 72: ...1 7 Storage Guidelines 72 YASKAWA TOEPYAIGA8001B GA800 Drive Maintenance Troubleshooting...
Page 336: ...4 10 Installation Methods 336 YASKAWA TOEPYAIGA8001B GA800 Drive Maintenance Troubleshooting...
Page 565: ...YASKAWA TOEPYAIGA8001B GA800 Drive Maintenance Troubleshooting 565...