Linear Technology DC257 Demo Manual Download Page 4

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DEMO MANUAL DC257

NO-DESIGN SWITCHER

QUICK START GUIDE

This demonstration board is easily set up to evaluate the
performance of the LTC1707 IC. Please follow the proce-
dure outlined below for proper operation.

• Refer to Figure 5 for proper connection of monitoring

equipment to ensure correct measurement.

• Connect the input power supply to the V

IN

 and GND

terminals on the left-hand side of the board. Do not
increase V

IN

 over 10V or the part will be damaged.

• Connect the load between the V

OUT

 and GND

terminals on the right side of the board.

• The RUN/SS pin can be left unconnected. To shut

down the LTC1707, tie this pin to GND.

• Set the desired output voltage with jumper JP1, as

shown in Figure 2 and Table 1.

JP1 POSITION

OUTPUT VOLTAGE

“1.5V”

1.51V

“1.8V”

1.82V

“2.5V”

2.52V

“2.9V

2.94V

“3.3V”

3.33V

“OPEN”

Figure 2. Output Voltage Selection (JP1)
(3.3V Position Shown)

1.8V

1.5V

2.5V

2.9V

3.3V

OPEN

JP1

DC257 F02

Table 1. Output Voltage Selection

OPERATIO

U

The circuit in Figure 1 highlights the capabilities of the
LTC1707. The application circuit is set up for a variety of
output voltages. Output voltages from 1.5V to 3.3V or user
programmable voltages can be obtained by selecting the
appropriate jumper position.

The LTC1707 is a monolithic synchronous step-down
switching regulator using a fixed-frequency architecture.
Burst Mode operation provides high efficiency at low load
currents. Operating efficiencies typically exceed 90% over
two decades of load current range. 100% duty cycle
provides low dropout operation, which extends operating
time in battery-operated systems.

Do not use small spring-clip leads when testing this
circuit. Soldered wire connections are required to properly
verify the performance of the PC board.

This demonstration board is intended for the evaluation of
the LTC1707 switching regulator IC and was not designed
for any other purpose.

The operating frequency of this demo circuit is 350kHz,
the frequency of the LTC1707’s internal oscillator. For
higher frequencies, SYNC/MODE (E8) can be synchro-
nized with an external clock. Burst Mode operation is
automatically disabled when the SYNC/MODE pin is ex-
ternally driven. Grounding SYNC/MODE also disables
Burst Mode operation, potentially reducing noise and RF
interference.

Soft-start is provided by an external capacitor, C

SS

, which

can be used to properly sequence supplies. The maximum
operating current level is 0.6A.

This demo board is optimized for 3.3V outputs and 5V
input. Output voltages from 1.5V to 3.3V are available by
selecting the appropriate position of JP1. For other output
voltages, select the OPEN position and add an appropriate
resistor value in the space provided. The output voltage
must never exceed 3.3V because the output capacitor may
be damaged. The input supply can range from 2.85V to
8.5V.

Summary of Contents for DC257

Page 1: ...reduce switching losses and maintain high operating efficiencies In switching noise sensitiveapplications BurstModeoperationcanbeinhib ited by grounding the SYNC MODE pin or synchronizing it with an external clock Gerber files for this circuit board are available Call the LTC factory SYMBOL PARAMETER CONDITIONS JUMPER POSITION VALUE VIN Input Voltage Range 2 85V to 8 5V VOUT Output Voltage See Fig...

Page 2: ...1 19V IREF Maximum VREF Output Currrent All 100µA Figure 1 LTC1707 Constant Frequency High Efficiency Converter Note 1 Programmable via optional R6 VOUT 0 8V 1 210k R6 PACKAGE A D SCHE ATIC DIAGRA S W U W 1 2 3 4 8 7 6 5 TOP VIEW VREF SYNC MODE VIN SW ITH RUN SS VFB GND S8 PACKAGE 8 LEAD PLASTIC SO LTC1707CS8 VFB GND ITH VIN SW 3 4 1 6 5 ITH VREF RUN SS 2 8 SYNC MODE 7 LTC1707 CC1 CSS 0 1µF CC2 47...

Page 3: ...000 JP1 1 22025 12 G1 0 079 Double Row Header COMM CON 626 301 4200 JP1 1 CCIJ2MM 138G 0 079 Center Shunt COMM CON 626 301 4200 L1 1 CD54 150MC 15µH 20 Inductor Sumida 847 956 0667 R1 1 CR16 2373FM 237k 1 1 16W Chip Resistor TAD 800 508 1521 R2 1 CR16 1653FM 165k 1 1 16W Chip Resistor TAD 800 508 1521 R3 1 CR16 9762FM 97 6k 1 1 16W Chip Resistor TAD 800 508 1521 R4 1 CR16 7872FM 78 7k 1 1 16W Chip...

Page 4: ...ixed frequency architecture Burst Mode operation provides high efficiency at low load currents Operatingefficienciestypicallyexceed90 over two decades of load current range 100 duty cycle provides low dropout operation which extends operating time in battery operated systems Do not use small spring clip leads when testing this circuit Solderedwireconnectionsarerequiredtoproperly verify the perform...

Page 5: ...atch andturnedoffwhenthecurrentcomparator ICOMP resets the RS latch The peak inductor current at which ICOMP resets the RS latch is controlled by the voltage on the ITH pin which is the output of error amplifier EA The VFB pin allows EA to receive an output feedback voltage from an externalresistivedivider Whentheloadcurrentincreases it causes a slight decrease in the feedback voltage relative to ...

Page 6: ...igh To disable Burst Mode operation and enable PWM pulse skipping mode connect the SYNC MODE pin to GND When the converter uses Burst Mode operation the peak current of the inductor is set to approximately 200mA even though the voltage at the ITH pin indicates a lower value The voltage at the ITH pin drops when the inductor s average current is greater than the load requirement As theITHvoltagedro...

Page 7: ...e compensation provides stability by preventing sub harmonicoscillations Itworksbyinternallyaddingaramp to the inductor current signal at duty cycles in excess of 40 As a result the maximum inductor peak current is lowerforVOUT VIN 0 4thanwhenVOUT VIN 0 4 Seethe maximum inductor peak current vs duty cycle graph in Figure 4 The graph labeled With External Clock shows the worst case peak current red...

Page 8: ... 432 1900 DC257 F06 10Ω OPERATIO U This applies to line regulation input to output voltage regulation as well as load regulation tests In doing the line regulation tests always look at the input voltage across the input terminals For the purposes of these tests the demonstration circuit should be powered from a regulated DC bench supply so that variations on the DC input do not add errors to the r...

Page 9: ...rom VIN by gradually increasing the internal current limit Power sup ply sequencing can also be accomplished using this pin An internal 2 25µA current source charges an external capacitor CSS When the voltage on RUN SS reaches 0 7V the LTC1707 begins operating As the voltage on RUN SS continues to increase from 0 7V to 1 8V the internalcurrentlimitalsoincreasesataproportionallinear rate The curren...

Page 10: ...10 DEMO MANUAL DC257 NO DESIGN SWITCHER W PCB LAYOUT A U D FIL Component Side Solder Mask Component Side Component Side Silkscreen ...

Page 11: ... believed to be accurate and reliable However no responsibility is assumed for its use Linear Technology Corporation makes no represen tationthattheinterconnectionofitscircuitsasdescribedhereinwillnotinfringeonexistingpatentrights W PCB LAYOUT A U D FIL Pastemask Solder Side Solder Side Solder Mask ...

Page 12: ...CIFIED 1 MATERIAL FR4 OR EQUIVALENT EPOXY 2 OZ COPPER CLAD THICKNESS 0 062 0 006 TOTAL OF 2 LAYERS 2 FINISH ALL PLATED HOLES 0 001 MIN 0 0015 MAX COPPER PLATE ELECTRODEPOSITED TIN LEAD COMPOSITION BEFORE REFLOW SOLDER MASK OVER BARE COPPER SMOBC 3 SOLDER MASK BOTH SIDES USING SR1020 OR EQUIVALENT 4 SILKSCREEN USING WHITE NONCONDUCTIVE EPOXY INK 5 ALL DIMENSIONS IN INCHES 6 SCORING 0 017 SYMBOL A B...

Page 13: ...Mouser Electronics Authorized Distributor Click to View Pricing Inventory Delivery Lifecycle Information Analog Devices Inc DC257A ...

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