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Flight Manual DG-1000M 

Issued: July 2014 

TN1000/23 

EASA app. 4.33 

Copyright DG Flugzeugbau GmbH - any copy or publishing prohibited

 

 

4.6

 

Flight with the engine removed from the aircraft 

The DG-1000M can be flown without the engine when the engine is sent 
for a major overhaul, or removed to decrease the aircraft empty weight for 
competition flying or for aerobatics. 
The following items must be executed: (see sect. 4.10.9 in the maintenance 
manual). 
 

1.

 

Remove the powerplant. Spindle drive, gas struts and exhaust system 
remain in the fuselage. 
Insulate the terminal of the starter motor positive wire (in the engine 
compartment). 

 
2.

 

In addition to the on-board battery install a battery in the fin see section. 
7.17.6. 

 

3.

 

Carry out a C.G. calculation according to section 6.9. The in-flight C.G. 
will be moved forward by approx. 75 mm (3 in.) depending on the 
flight mass and empty mass C.G. 
This C.G. shift is acceptable, as the forward limit of the in-flight C.G. 
for operation with engine removed is 120 mm in front of the C.G. with 
engine installed. 

Item mass 

C.G. 

behind 

datum 

moment 

  

kg 

 lbs. 

m  

ft. 

kg×m  ft.×lbs.

Mass reduction 

engine with propeller 

-58 

-127.9

1.261 

4.14  -73.14  -529.0 

Additional mass 

fin battery 

5.5 

12.1 

5.34 

17.52  29.37 

212.4 

Difference -52.5 

-115.7

0.834 

2.735 

-43.77 

-316.6 

 
4.

 

Fix the limit switch “engine retracted” with a Ty-rap in the actuated 
position. Otherwise the DEI-NT will remain in the powered flight 
mode. 

5.

 

Tape the engine doors carefully with fabric tape. 

 

Note:

 After switching on the main switch some failure messages will be 

displayed. Confirm each message by pressing the selector switch to eliminate 
the message. 
 

 

Summary of Contents for DG-1000M

Page 1: ...age will be indicated by a black vertical line in the right hand margin and the under lying document for the revision and the date will be shown on the bottom of the page Rev No Affected Pages section...

Page 2: ...ctober 2010 October 2012 1 6 October 2010 2 EASA app 2 1 October 2010 2 2 October 2010 2 3 October 2010 2 4 October 2010 2 5 October 2010 October 2012 July 2014 2 6 October 2010 July 2014 2 7 October...

Page 3: ...ctober 2012 4 16 October 2010 4 17 October 2010 4 18 October 2010 4 19 October 2010 4 20 October 2010 4 21 October 2010 October 2012 4 22 October 2010 4 23 October 2010 4 24 October 2010 October 2012...

Page 4: ...2 6 13 October 2012 6 14 October 2012 6 15 October 2012 7 7 1 October 2010 7 2 October 2010 October 2012 7 3 October 2010 7 4 October 2010 7 5 October 2010 7 6 October 2010 October 2012 7 7 October 20...

Page 5: ...ignition If you reduce the engine speed the ignition will be activated again Note The max engine RPM given by the engine manufacturer is 6700 RPM This max RPM is reduced for operation in the DG 1000M...

Page 6: ...s Limitation data for the non useable amount of fuel printed above the display red 1 L When a fuel quantity of approx 4 Litres is reached a full screen warning Low Fuel appears when this warning has b...

Page 7: ...Carry out a C G calculation according to section 6 9 The in flight C G will be moved forward by approx 75 mm 3 in depending on the flight mass and empty mass C G This C G shift is acceptable as the f...

Page 8: ...retracted e g on the trailer after derigging after 60 seconds With landing gear extended e g in the hangar after 5 minutes In both cases time counts after the last operation of any item of the electri...

Page 9: ...0 12 V min 12 Ah mass 5 5 kg 12 1 lbs is permitted The battery fuse is installed at the battery type G fuse G 250 V 5 x 20 4 A fast The wiring for this battery is in parallel to the battery in the bag...

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