Cause
Possible Solutions
Undervoltage was detected.
• Check the drive input power voltage by looking at the DC bus voltage (U1-07).
• Check all main circuit wiring.
u
Motor Does Not Rotate Properly after Pressing AUTO Button or after Entering External
Run Command
n
Motor Does Not Rotate
Cause
Possible Solutions
The drive is not in the Drive Mode.
• Check if the DRV light on the HOA keypad is lit.
• Enter the Drive Mode to begin operating the motor.
Refer to The Drive and Programming Modes on page 99
HAND
was pushed.
Stop the drive and check if the correct frequency reference source is selected. If the operator keypad shall be the
source, the LO/RE button LED must be on. If the source is REMOTE, it must be off.
Take the following steps to solve the problem:
•
Push
HAND
.
Auto-Tuning has just completed.
• When Auto-Tuning completes, the drive is switched back to the Programming Mode. The Run command will
not be accepted unless the drive is in the Drive Mode.
• Use the HOA keypad to enter the Drive Mode.
Refer to The Drive and Programming Modes on page 99
.
A Fast Stop was executed and has
not yet been reset.
Reset the Fast Stop command.
Settings are incorrect for the source
that provides the Run command.
Check parameter Z1-08 (Run Command Selection).
Set Z1-08 so that it corresponds with the correct Run command source.
0: HOA keypad
1: Control circuit terminal (default setting)
2: MEMOBUS/Modbus communications
3: Option card
There is faulty wiring in the control
circuit terminals.
• Check the wiring for the control terminal.
• Correct wiring mistakes.
• Check the input terminal status monitor (U1-10).
The drive has been set to accept the
frequency reference from the
incorrect source.
Check parameter b1-01 (Frequency Reference Selection 1).
Set b1-01 to the correct source of the frequency reference.
0: HOA keypad
1: Control circuit terminal (default setting)
2: MEMOBUS/Modbus communications
3: Option card
The terminal set to accept the main
speed reference is set to the incorrect
voltage and/or current.
If the frequency reference is set at terminal A1, check parameter H3-01 for the correct signal level selection. If
terminal A2 is used, check parameter H3-09.
Refer to Input Signal Selection for Terminals A1 and A2 on page
Selection for the sink/source mode
and the internal/external power
supply is incorrect.
Check wire jumper connection between terminals SC and SP.
Frequency reference is too low.
Check the frequency reference monitor (U1-01).
Multi-function analog input is set up
to accept gain for the frequency
reference, but no voltage (current)
has been provided.
• Check the multi-function analog input settings.
• Check if analog inputs A1 or A2 are set for frequency reference gain (H3-02, H3-10 = 1). If so, check if the
correct signal is applied to the terminal. The gain and the frequency reference will be 0 if no signal is applied to
the gain input.
• Check if H3-02 and H3-10 have been set to the proper values.
• Check if the analog input value has been set properly. (U1-13 and U1-14)
OFF
was pressed when the
drive was started from a REMOTE
source.
•
Pressing
OFF
will decelerate the drive to stop.
• Switch off the Run command and then re-enter a new Run command.
•
Set o2-02 to 0 to disable
OFF
.
Motor starting torque is too low.
Refer to Motor Performance Fine-Tuning on page 224
Frequency reference value is too low
or the drive does not accept the value
entered.
Enter a value that is above the minimum output frequency determined by E1-09.
6.9 Troubleshooting without Fault Display
YASKAWA ELECTRIC SIEP YAIZ1B 01E YASKAWA AC Drive – Z1000 Bypass Technical Manual
259
6
Diagnostics & Troubleshooting
Содержание Z1000 CIMR-ZU*A Series
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