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YASKAWA
SIEPC71061753A GA500 Technical Manual
255
Code
Name
Causes
Possible Solutions
oL4
Overtorque Detection 2
A fault occurred on the machine.
Example: The machine is locked.
Examine the machine and remove the cause of the fault.
The parameters are incorrect for the load.
Adjust
L6-05 [Torque Detection Level 2]
and
L6-06 [Torque
Detection Time 2]
settings.
Note:
•
The drive detects this fault if the drive output current is more than the level set in
L6-05
for longer than
L6-06
.
•
Do a Fault Reset to clear the fault.
•
If the drive detects this fault, it will operate the motor as specified by the Stopping Method set in
L6-04 [Torque Detection Selection 2]
.
•
L5-07 [Fault Reset Enable Select Grp1]
disables the Auto Restart function.
Code
Name
Causes
Possible Solutions
oL5
Mechanical Weakening Detection 1
The drive detected overtorque as specified by the
conditions for mechanical weakening detection set
in
L6-08 [Mechanical Fatigue Detect Select]
.
Do a deterioration diagnostic test on the machine side.
Note:
•
Do a Fault Reset to clear the fault.
•
If the drive detects this fault, it will operate the motor as specified by the Stopping Method set in
L6-08
.
Code
Name
Causes
Possible Solutions
oL7
High Slip Braking Overload
The load inertia is too large.
An external force on the load side rotated the motor.
Something is preventing deceleration on the load
side.
•
Decrease deceleration times in
C1-02, C1-04, C1-06, and C1-
08 [Deceleration Times]
for applications that do not use High
Slip Braking.
•
Use a braking resistor to decrease the deceleration time.
The value set in
n3-04 [HSB Overload Time]
is too
small.
•
Increase the value set in
n3-04
.
•
Connect a thermal overload relay to the motor, and set
n3-04 =
1200 s (maximum value)
.
Note:
•
The drive detects this fault if the output frequency is constant for longer than
n3-04
.
•
Do a Fault Reset to clear the fault.
Code
Name
Causes
Possible Solutions
oPr
Keypad Connection Fault
The keypad is not securely connected to the
connector on the drive.
Examine the connection between the keypad and the drive.
The connection cable between the drive and the
keypad is disconnected.
•
Remove the keypad and then reconnect it.
•
Replace the cable if damaged.
Note:
•
The drive detects this fault if these conditions are correct:
–
o2-06 = 1 [Keypad Disconnect Detection = Enabled]
.
–
b1-02 = 0 [Run Command Selection 1 = Keypad]
, or the drive is operating in LOCAL Mode with the keypad.
•
Do a Fault Reset to clear the fault.
Code
Name
Causes
Possible Solutions
oS
Overspeed
There is overshoot.
•
Decrease
C5-01 [ASR Proportional Gain 1]
and increase
C5-
02 [ASR Integral Time 1]
.
•
Use
H6-02 to H6-05 [Pulse Train Input Setting Parameters]
to
adjust the pulse train gain.
There is an incorrect number of PG pulses set in the
drive.
Set
H6-02 [Terminal RP Frequency Scaling]
to the pulse train
frequency during 100% reference (maximum motor rotation
speed).
The
oS
detection level is set incorrectly.
Adjust
F1-08 [Overspeed Detection Level]
and
F1-09 [Overspeed
Detection Delay Time]
.
If the drive detects the fault at start or in the low
speed range (10% or less) and
n8-57 = 1 [HFI
Overlap Selection = Enabled]
for PM Control
methods, the high frequency injection gain is too
high.
•
Set
E5-xx [PM Motor Parameters]
correctly or do Rotational
Auto-Tuning.
•
Decrease the value of
n8-41 [HFI P Gain]
in 0.5 unit
increments.
Note:
Set
n8-41 > 0.0
for IPM motors.
Note:
•
The drive detects this fault if the motor speed is more than the value set in
F1-08
for longer than
F1-09
.
•
Do a Fault Reset to clear the fault.
•
If the drive detects this fault, it will operate the motor as specified by the Stopping Method set in
F1-03 [Overspeed Detection Selection]
.
Code
Name
Causes
Possible Solutions
ov
Overvoltage
The deceleration time is too short and too much
regenerative energy is flowing back into the drive.
•
Increase the values set in
C1-02, C1-04, C1-06, or C1-08
[Deceleration Times]
.
•
Connect a dynamic braking option to the drive.
•
Perform Deceleration Rate Tuning.
The acceleration time is too short.
•
Make sure that sudden drive acceleration does not cause the
fault.
•
Increase the values set in
C1-01, C1-03, C1-05, or C1-07
[Acceleration Times]
.
•
Increase the value set in
C2-02 [S-Curve Time @ End of
Accel]
.
•
Set
L3-11 = 1 [Overvoltage Suppression Select = Enabled]
.
Содержание CIPR-GA50C series
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Страница 12: ...12 YASKAWA SIEPC71061753A GA500 Technical Manual...
Страница 44: ...2 9 Installation Methods 44 YASKAWA SIEPC71061753A GA500 Technical Manual...
Страница 110: ...3 17 Motor Application Precautions 110 YASKAWA SIEPC71061753A GA500 Technical Manual...
Страница 150: ...4 12 Test Run Checklist 150 YASKAWA SIEPC71061753A GA500 Technical Manual...
Страница 156: ...5 2 European Standards 156 YASKAWA SIEPC71061753A GA500 Technical Manual...
Страница 157: ...Standards Compliance 5 5 2 European Standards YASKAWA SIEPC71061753A GA500 Technical Manual 157...
Страница 158: ...5 2 European Standards 158 YASKAWA SIEPC71061753A GA500 Technical Manual...
Страница 159: ...Standards Compliance 5 5 2 European Standards YASKAWA SIEPC71061753A GA500 Technical Manual 159...
Страница 288: ...7 10 Troubleshooting Without Fault Display 288 YASKAWA SIEPC71061753A GA500 Technical Manual...
Страница 306: ...8 6 Storage Guidelines 306 YASKAWA SIEPC71061753A GA500 Technical Manual...
Страница 454: ...11 22 Parameters Changed by PM Motor Code Selection 454 YASKAWA SIEPC71061753A GA500 Technical Manual...