is above the
not connected
sharply differs from
he output is
Fault Tracking
115
Fault code
Fault type
Possible cause
What to do
EEP
EEPROM fault
Error of controlling the write
and read of the parameters
Damage to EEPROM
Press STOP/RST to reset
Change the main control
panel
PIDE
PID feedback fault
PID feedback offline
PID feedback source
disappear
Check the PID feedback
signal
Check the PID feedback
source
bCE
Braking unit fault
Braking circuit fault or
damage to the braking
pipes
The external braking
resistor is not sufficient
Check the braking unit and
change new braking pipe
Increase the braking
resistor
ETH1
Grounding shortcut
fault 1
T
short circuited
with the ground
There is fault in the current
detection circuit
The actual motor power
power.
Check if the connection of
the motor is normal or not
Change the hall
Change the main control
panel
Set motor parameters
correctly.
ETH2
Grounding shortcut
fault 2
dEu
Velocity deviation
fault
The load is too heavy or
stalled
Check the load and ensure
it is normal
Increase the detection time
Check whether the control
parameters are normal
STo
Maladjustment fault
The control parameters of
the synchronous motors not
set properly
The autotune parameter is
not right
to the motor
Check the load and ensure
it is normal
Check whether the control
parameter is set properly or
not
Increase the maladjustment
detection time
END
Time reach of
factory setting
The actual running time of
internal setting
running
time
Ask for the supplier and
adjust the setting running
time
PCE
Keypad
communication
fault
The connection of the
keypad wires is not good or
broken
The keypad wire is too long
and affected by strong
Check the keypad wires
and ensure whether there is
mistake
Check the environment and
avoid the interference